I carefully covered everything that I didn't want to be covered with swarf and then started to drill a pilot hole of 4mm As soon as it was a couple of millimeters deep I carefully rotated the drill to the correct angle to line up with the groove in the pulley and completed the hole.
This was then followed with a 20mm diameter hole saw which had its own pilot of 8mm diameter. As before i started the drill and after a few mm aligned it with the 4mm pilot hole. This made getting it all aligned a little easier. I had to be very careful as the hole saw started to cut into the plate as it was just a one sided cut so all had to progress slowly and carefully. The hole saw atr through the chassis plate much better than hoped and I have ended up with a pretty tight hole for the adapter tube.
Next I had to cut the slot for the cable. This was a labouious job and painfully slow. I ended up chain drilling a 4mm hole and using the drill as a slot drill to join all the holes up. Filing the slot was also really slow as access is tricky. Still got a little to do to make all smooth and straight (I'm a bit OCD as all has to be true and straight!).
Template added to chassis. Looks tight!!! |
Drilling with the 20mm diameter hole saw. All covered. |
Hole completed. |
Slot added. Now just to angle and clean up. |
Only thing's to do now is to weld in the adapter, clean up and repaint the whole area.
On the whole I am really pleased with the progress, just need to get that welder!!!
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